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Old 11-25-2013, 05:49 PM
wildbob wildbob is offline
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Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
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I agree 351, spraying carb cleaner around the seals on carb, manifold, intake didn't seem to change anything but I'll try to re-seat and tighten down again and see if that helps. I was assuming the initial bogging was the pumper dumping fuel the motor couldn't handle standing still to WOT. I realize the 30mm pumper is probably too much carb right now, but if I go light till it just starts rolling THEN nail it, it SPINS the rears and takes off like a mad man. On a fairly straight stretch where I'd get to about 28-30MPH, she was at 35 and still pulling.. FYI 35 pilot 135 main @ sea level with 110 Octane leaded racing fuel.
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2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B

Last edited by wildbob; 11-25-2013 at 05:51 PM.