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  #1  
Old 03-11-2013, 09:09 AM
bwomack524 bwomack524 is offline
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Default not wanting to ideal

My yerf dog is not wanting to ideal. It started this the last time I took it out not wanting to start or odeal. I took apart the carb this weekend because it had been sitting for a little bit. It seem to run good after I clean the carb but something is not right any ideals?. I have that stage 1 red neck kit on it
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Old 03-11-2013, 09:09 AM
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sorry I meant idle
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Old 03-11-2013, 12:53 PM
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Default Check it all

check all your hoses for signs of cracks or dry rotting, also check the petcock/diapham to make sure its good to go! If thats not it, you just have to go thru it all make sure your carb intake is thight also! hope this helps
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Old 03-11-2013, 06:15 PM
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Also check for air leaks.
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Old 03-13-2013, 09:08 AM
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If the vent on the valve cover is plugged will that cause it not to idle? Its the only tubing that I found to be dry rotted. I havent had a chance to check on the rubber intake for crachs yet
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Old 03-13-2013, 09:36 AM
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Not to my knowledge, but I could be wrong, maybe someone else will chime in!
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Old 03-13-2013, 12:36 PM
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Maybe check your pilot air screw.
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Old 03-13-2013, 02:45 PM
bwomack524 bwomack524 is offline
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where is the air screw located? When I had the carb apart I did clean the pilot jet but didnt mess with the mixture screw. Its suppose to be 3 turns out right?
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Old 03-13-2013, 03:07 PM
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I am not sure because I don't have a yerf dog. I was throwing the idea out there.
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Old 03-13-2013, 05:49 PM
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3 turns sounds pretty close, mine was around 4.5 to 5 with BW air intake installed. If this is a spiderbox, the screw should be on the left side, close to the exit of the carb main body, and can be a pain to get at, and that screw controls the fuel, not air mix, so in would be leaning the mix out, and out would fatten it up.
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Old 03-14-2013, 12:15 AM
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Did your buggy idle before the intake and did you oil the filter?
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Old 03-14-2013, 04:05 PM
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Quote:
Originally Posted by bwomack524 View Post
If the vent on the valve cover is plugged will that cause it not to idle? Its the only tubing that I found to be dry rotted. I havent had a chance to check on the rubber intake for crachs yet
The vent should not be plugged it is meant to breath so that pressure will not build up in the crankcase. I don't think it would affect the idle but it would definitely not be good to run high rpm like that. That being said, you may need to adjust the a/f mix screw. best way is to adjust the idle speed to where it will run (around 1000 rpms is good) and adjust in or out 1/4 turn at a time, giving 15 seconds for adjustment to take affect.While adjusting you want the rpms to rise with each adjustment not go down. If adjustments cause rpms to lower then adjust screw the other way. Keep adjusting until the rpms are at highest point. From there a 1/2 turn in either direction should cause rpms to drop. This how you know you are in the right spot. Then adjust your idle speed where you want it.
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Old 03-14-2013, 04:09 PM
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Default screw location

This is looking from "drivers" side
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Old 03-23-2013, 09:18 PM
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I've replaced the hoses and the intake and its still doing the same. It will take several time to even get it to try to start. When it finally does it runs then dies and I have to keep playing to keep it running. When it finally runs it seem to run good with no back firing when I let off from running wide open. But even after that it will not idle and is hard to get it to start again. I'm missing something. It also seems like it doesn't have as fast of the rev. As it use to. I will try the mixer screw and see what happens. It was running great before I let it sit a while
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Old 03-24-2013, 07:38 AM
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What engine do you have?
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Old 03-24-2013, 10:10 AM
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Howhitt 150cc 04 model with the stage 1 redneck upgrade
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Old 03-24-2013, 12:28 PM
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Have you checked compression or valve lash settings??
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  #18  
Old 03-24-2013, 05:06 PM
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It runs fine once I get it started. Doesn't miss a beat
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Old 03-25-2013, 07:14 AM
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Could be valves off just enough to affect it when it's cold but even out when warmed up. Could be a cracked spark plug or corroded or loose connections somewhere.Could be the CDI or the coil. Just have to go through it with a fine toothed comb at this point.
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http://www.youtube.com/watch?v=3hx-hEWl10c
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Old 03-25-2013, 08:58 AM
bwomack524 bwomack524 is offline
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Your right Im going to start at the beginning. Take and clean the carb one more time and then go from there. Could it be the clutch dragging a little? Also to me on the carb it is looking like its not getting enough fuel. I have all new from the fuel tank to the carb so it should be enough fuel
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Old 03-25-2013, 11:06 AM
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Is your battery good? Is it cranking fast enough?
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Old 03-25-2013, 11:16 AM
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yes the battery good . I have a 12v battery from an electric wheelchair on it
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Old 03-25-2013, 11:36 AM
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Check the pilot jet to make sure you can see light through it. Your air fuel adjustment should be 1-1 1/2 turns out 3-4 turns indicate the idle circuit is lean. Have you done a rejet when you went with the UNI?
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Old 03-25-2013, 01:15 PM
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Yes I forgot what size jets but after I put them in it ran great. I cleaned the pilot jet before but it might have got plugged again. That my next step ic checking and recleaning the carb
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Old 04-01-2013, 01:54 PM
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yaa got her running. The only strange thing is that I am not finding fuel/air mixing screw. are some preset from factory
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Old 04-01-2013, 10:41 PM
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Left ( drivers side) of carb just above fuel bowl intake end.
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  #27  
Old 04-02-2013, 08:02 AM
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Mine was coated with a hardened glue that made it difficult to notice and had to be temoved in order to adjust.
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SYC Perf head P&P,Matched intake and exhaust, A12 cam, Orange CDI & coil, Motorio pulley, 115mm Variator and lightweight drive face,11gm Sliders, UNI, modded muffler + 200 horsepower

http://www.youtube.com/watch?v=3hx-hEWl10c
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Old 04-02-2013, 11:48 AM
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Yerfdog's did not fall under the epa guides at the time. He should not have a plugged air/fuel mix screw. EPA required plugging of the A/F mix screw in 2008.
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Old 04-02-2013, 12:07 PM
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EPA= Everyones Perfect Adversary. So that blew my idea out of the water.
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SYC Perf head P&P,Matched intake and exhaust, A12 cam, Orange CDI & coil, Motorio pulley, 115mm Variator and lightweight drive face,11gm Sliders, UNI, modded muffler + 200 horsepower

http://www.youtube.com/watch?v=3hx-hEWl10c
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Old 04-02-2013, 12:37 PM
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Unless the carb has been replaced, I have heard of some who ordered a new carb online and come to them plugged but this is not the norm. The supplier of buggies can only sell the epa approved carbs, ie. Hammerhead, trailmaster ect. Private suppliers of parts do not.
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Old 04-02-2013, 01:45 PM
bwomack524 bwomack524 is offline
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Mine is plugged so there is a scew under the plug and is it hard to get the plug off?
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