BuggyMasters.Com - An On Line Mini Buggy Forum and Go Kart Forum

Go Back   BuggyMasters.Com - An On Line Mini Buggy Forum and Go Kart Forum > Technical Discussions > 150cc GY6 and Under Engine Tech

150cc GY6 and Under Engine Tech GY6 and Smaller Technical Discussion Forum

Reply
 
Thread Tools
  #1  
Old 01-03-2011, 01:09 PM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default Carbide 150

Just bought one for the kids. Worked perfect for a week and then right in the middle of operation it bogged down and died. It will start and idle just fine but when you give it gas it acts like it floods out and dies. You can slowly idle it up a little but only for a brief time. I'm not very bright on these machines. Any help is appreciated.
Reply With Quote
  #2  
Old 01-03-2011, 06:16 PM
olderthan's Avatar
olderthan olderthan is offline
Heavy Contributor
 

Join Date: Jan 2010
Location: dayton nev--lake tahoe,nv
Posts: 588
Default

pull carb & clean the jets
__________________
olderthan
2008 tomberline punisher
1500 spring 12g sliders
30mm cv pumper carb
uni filter no rev cdi
polaris xlt snowmobile shocks for front
w/550 magnum springs & blaster fronts on rear
and another buggy built working on mods gk-13
white spring 17 gram sliders so far
Reply With Quote
  #3  
Old 01-04-2011, 07:53 AM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default

I pulled the bowl off carb and loked at the jets, I pulled the fuel filter off and checked it, I pulled the auto choke off and checked it, I checked the air filter. Nothing seemed to work after trying each of these. As I was fixing to give up for the night it kicked off and started working so I have no idea what I did to fix it.
Reply With Quote
  #4  
Old 01-04-2011, 06:02 PM
metalstudman1's Avatar
metalstudman1 metalstudman1 is offline
Super Moderator
 

Join Date: Aug 2009
Location: Belmont,NC (elevation 534')
Posts: 2,668
Default

You'd be amazed at what a very small piece of trash floating around in the carb can do to your perfectly running engine, it get's dislodged and then runs bad again.Blowing out all the orifices & jets out with compressed air to make sure it's clear.A simple disconnect and reconnection of a wire can fix things as well. I'm glad it's working now for you.

Last edited by metalstudman1; 01-05-2011 at 02:44 PM.
Reply With Quote
  #5  
Old 01-05-2011, 07:22 AM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default

Thanks for the help. I read a lot of the posts on this site to figure out what to try and it was very informative. This site is great for anyone who has a buggy. My 4 kids love the machine so I am sure I will be on here often. Thanks for the replies.
Reply With Quote
  #6  
Old 01-08-2011, 06:09 PM
robbieo1973 robbieo1973 is offline
Lurker
 

Join Date: Jan 2011
Posts: 4
Default

yup i did that on the one i just bought
i bought it with reading what i have seen on this fourm abou the carb debise issue.
so it idled fine went to gas it and she would die store discounted it by 300 and sold it to me also gave me 10% off the gear i bought so it was a win for all 1/2hour after it was home snow was being thrown by tires yahooooooooooooo
Reply With Quote
  #7  
Old 01-10-2011, 07:57 AM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default

Well she went down again this weekend. It repeated the same failure. I noticed that I am using a lower octane gas than I wa suppose to. I am going to drain it and get the right octane. Could that be the issue? Could it have been dirt in the tank that keeps clogging it up or could it have been the same piece of trash that originally shut it down?
Reply With Quote
  #8  
Old 01-10-2011, 08:16 AM
robbieo1973 robbieo1973 is offline
Lurker
 

Join Date: Jan 2011
Posts: 4
Default

sorry yes to all of them it is a fuel issue also done u smell unburnt gas at the exhaust might neeed to adjust carb looking from rear of machine it is on left it is the LOWER silver cap near front of carb book says 21/4-2/34 turns is what it should be
Reply With Quote
  #9  
Old 01-10-2011, 10:45 AM
GX150's Avatar
GX150 GX150 is offline
Heavy Contributor
 

Join Date: Dec 2010
Posts: 645
Default

A 24mm carburetor should be 1.5 turns out from fully seated. The directions you posted are for the 28-32mm carburetors typical on 250's.
Reply With Quote
  #10  
Old 01-10-2011, 12:47 PM
metalstudman1's Avatar
metalstudman1 metalstudman1 is offline
Super Moderator
 

Join Date: Aug 2009
Location: Belmont,NC (elevation 534')
Posts: 2,668
Default

If I were still having this issue I'd be pulling the carb and blowing it out AGAIN!!!The octane level shouldn't cause a failure of this type you're having but a lack of performance only.Have you got an in-line fuel filter?When you disconnect the fuel line from the carb- does the fuel flow well?Trash from the tank isn't likely going to get past the filter but clog it up first.
Reply With Quote
  #11  
Old 01-10-2011, 08:54 PM
PAbuggy's Avatar
PAbuggy PAbuggy is offline
Lite Contributor
 

Join Date: Mar 2010
Location: dubois PA
Posts: 47
Default

I would junk the factory vacumm petcock and put on a inline this could be your problem its a cheap fix and will give you less trouble down the road.
__________________
asw carbide 1500 main and clutch springs HP clutch and bell koso variator performance cdi uni redneck intake fmf exaust 9gram rollers 39 tooth sprocket 140main and 40 pilot jet
Reply With Quote
  #12  
Old 01-10-2011, 09:49 PM
wasjustlooking's Avatar
wasjustlooking wasjustlooking is offline
Lite Contributor
 

Join Date: Dec 2010
Location: Friendsville TN
Posts: 34
Default

Take a look at the inside of the gas cap. The ethanol in gas has been bad about melting the inside of these caps closing off the vent so no air gets into the tank.
__________________
08 Joyner SV 250 17grm sliders,white main spring,UNI,130 main,40 pilot,22x810 Kenda Front Max,23x10x10 ITP Muddlites
08 ASW Carbide (my son's)Lots of mods
Reply With Quote
  #13  
Old 01-17-2011, 03:40 PM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default

I pulled the carb and took the bowl off, blew out the jets and put new gas in it. SO far it is running. The kids were gone this weekend so it hasn't seen but about an hour and a half of running. At least this time when it was put back in the garage it wasn't being pushed. Thanks for the help. I hope its at least a month or so before I have to ask any more questions.
Reply With Quote
  #14  
Old 01-21-2011, 10:41 AM
JDbuggyman JDbuggyman is offline
Lurker
 

Join Date: Jan 2011
Posts: 3
Default

Brad, I'm having the same problem with my Kazuma 150.
What size main jet are you running?
I found a 95 in mine and from reading other similar posts, it sounds like replacing the 95 with a 108 should eliminate this condition where the unit dies after a quarter throttle. If you are running a 95, I was just wondering if you actually got a full range of throttle when it does run?
I'm stopping tonight to pick up some larger jets for mine, I'll reply after I've installed and tested them.
Thanks.
Reply With Quote
  #15  
Old 01-21-2011, 11:37 AM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default

From what I have read I have a 95 in mine also. I didn't take it out and measure it. My kids got out of school yesterday and played in the snow with it a couple of times and both times it stayed running. They drove it until they couldn't handle the cold. Does changing sizes keep it from clogging as bad? I also put a higher octane gas than the gas I run in my mower which I was using when it went down.
Reply With Quote
  #16  
Old 01-21-2011, 08:39 PM
wasjustlooking's Avatar
wasjustlooking wasjustlooking is offline
Lite Contributor
 

Join Date: Dec 2010
Location: Friendsville TN
Posts: 34
Default

Most carbides come with a 114 main and 34 pilot. Even for a stock engine they are too small and if you do some test runs with a new plug and shut the engine off at w.o.t. you will most likely find it is running lean. The factory installs the smaller jets to meet emmission standards. A 120 main and slightly larger pilot might solve the problem for good. The size is stamped on the top or side of the jets. Replacing the vaccum petcock with a fuel shut-off is a good idea. It's just a problem waiting to happen.
__________________
08 Joyner SV 250 17grm sliders,white main spring,UNI,130 main,40 pilot,22x810 Kenda Front Max,23x10x10 ITP Muddlites
08 ASW Carbide (my son's)Lots of mods
Reply With Quote
  #17  
Old 01-24-2011, 07:59 AM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default

Well my luck is bad or I have a lemon. The cart is running super right now, the nuts on the exhaust vibrated off and that had to be fixed but wasn't to bad. But now it sounds like I have rocks inside my transmision. Sounds like something broke loose and is rattling around in there. It still runs good but sounds horrible. Sounds like it is going to have to go in for warranty work.
Reply With Quote
  #18  
Old 01-24-2011, 04:59 PM
chuckorlando chuckorlando is offline
Contributor
 

Join Date: Apr 2010
Posts: 356
Default

You sure the exhaust gasket did'nt fall out? If it is the cvt you probly somehow broke a junk of belt, vari fin, or a roller got loose.

If you or someone has had the cvt apart then you probly spun the vari or clutch nut lose
Reply With Quote
  #19  
Old 01-27-2011, 03:45 PM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default

The service guy said something had broke loose in the transmission. Wasn't a belt. Its under warranty so he is going to replace it. American SportWorks is going to warranty the replacement so it will be all good if it doesn't take to long.
Reply With Quote
  #20  
Old 02-28-2011, 02:59 PM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default

Well I am still waiting on SportWorks to send the replacement transmission. I am starting to get a little aggravated. I bought a new 150 that my kids got to ride 10 days after Christmas and now its almost March. Maybe there slowplaying me trying to let the warranty run out. The Carbide is getn a bad name around my neighborhood just for the fact I have to tell everyone its broke down when they ask. Frustrating.
Reply With Quote
  #21  
Old 02-28-2011, 03:08 PM
GX150's Avatar
GX150 GX150 is offline
Heavy Contributor
 

Join Date: Dec 2010
Posts: 645
Default

Most of the internal reverse units need an additional helper spring to keep the gear selection in forward. This issue started when the Baja Reaction was released and still has not been addressed by any of the manufacturers.
Attached Images
File Type: jpg Gearbox spring.JPG (85.3 KB, 20 views)
Reply With Quote
  #22  
Old 02-28-2011, 03:15 PM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default

Mine seems to run ok but whatever is bouncing around inside the transmission sounds like it could come exploding out and hurt one of my kids. I was going to let them ride it until it quit since I have been waiting since the first of January but safety was an issue for me.
Reply With Quote
  #23  
Old 02-28-2011, 07:20 PM
wasjustlooking's Avatar
wasjustlooking wasjustlooking is offline
Lite Contributor
 

Join Date: Dec 2010
Location: Friendsville TN
Posts: 34
Default

Call them over and over untill they get tired of hearing from you. ASW likes to drag their feet when it comes to warranty issues. They are a good cart, tough as nails. My son's takes a beating every time we go riding and still runs like a champ. Don't give up, make them get it done.
Attached Images
File Type: jpg 006-5.jpg (91.5 KB, 16 views)
__________________
08 Joyner SV 250 17grm sliders,white main spring,UNI,130 main,40 pilot,22x810 Kenda Front Max,23x10x10 ITP Muddlites
08 ASW Carbide (my son's)Lots of mods
Reply With Quote
  #24  
Old 03-21-2011, 01:48 PM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default

Got it fixed a week ago. The gears were chewed up something bad. We had to go out of town the next day so they didn't get to ride it. The day after we got back the kids got it out and ran it like crazy. Everything went great right up to where my little boy rolled it and broke his humerous bone. Not sure how since it rolled away from him but he is down for at least 8 weeks. What a deal Huh.
Reply With Quote
  #25  
Old 03-21-2011, 01:57 PM
BuggyMaster's Avatar
BuggyMaster BuggyMaster is offline
Administrator
 

Join Date: Jul 2009
Posts: 2,311
Default

ohhh mannnn!!!! Poor kid! Sadly, sometimes it takes something like this to gain the best experience.
Reply With Quote
  #26  
Old 03-21-2011, 02:00 PM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default

Yaa, he may still have to have surgery to line the bone back up. He has handled it very well. Were not getting rid of the cart. He may be a little slower next time but all the safety features were in place and he will be fine for football season.
Reply With Quote
  #27  
Old 03-23-2011, 08:45 AM
SYCARMS's Avatar
SYCARMS SYCARMS is offline
Supporting Vendor
 

Join Date: Sep 2009
Location: Senatobia, Mississippi
Posts: 3,375
Default

One thing you might want to pick up are arm restraints if you don't already have. These will keep the arms inside in case of rollover, alway's wear the belts adjusted properly and of coarse a helmet.Sorry to hear the bad news, hope he does not need surgery. Sometimes these things happen. Glad to hear your not dumping the buggy because of his misfortune, it could of happened on a bicycle as well.

TOM
Reply With Quote
  #28  
Old 03-23-2011, 08:55 AM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default

I have seen the arm restraints and have talked about getting them when I bought the buggy. Where can I get them adn are there several types?
Reply With Quote
  #29  
Old 03-23-2011, 09:20 PM
bam41's Avatar
bam41 bam41 is offline
Lite Contributor
 

Join Date: Dec 2010
Location: Wildersville, TN
Posts: 49
Default

wow, that sucks! Tell him to hang in there. Its really hard to keep those arms in the buggy during a roll over. Tom and his son had a roll over at the bash last year, Eric was video taping the ride when it happened. When they finished wrecking..., Eric was laying on Tom (he's no small boy either) and was still taping! You could almost hear Tom grunting! lol. Sorry Tom
__________________
2006 HH150.....kinda
prodigy vari/clutch 11g Rollers/Yellow Main
White Brothers Performance Pipe/No Rev CDI/Hot Coil
Stroker Crank/BB 180 kit
Mikuni VM28 - 35 Pilot - 140 Main
A12 cam
blaster shocks x4
vapor speedo
Reply With Quote
  #30  
Old 03-23-2011, 10:41 PM
SYCARMS's Avatar
SYCARMS SYCARMS is offline
Supporting Vendor
 

Join Date: Sep 2009
Location: Senatobia, Mississippi
Posts: 3,375
Default

That was actually our time to bind, and yes he is no small boy and not light either. Wait till you see him this year.

TOM
Reply With Quote
  #31  
Old 03-24-2011, 07:07 AM
Brad Brad is offline
Lurker
 

Join Date: Jan 2011
Posts: 14
Default

Is there any way to widen the stance of the buggy?
Reply With Quote
  #32  
Old 03-24-2011, 09:07 AM
SYCARMS's Avatar
SYCARMS SYCARMS is offline
Supporting Vendor
 

Join Date: Sep 2009
Location: Senatobia, Mississippi
Posts: 3,375
Default

Wheel spacers but in our case it would not have made a differance.

TOM
Reply With Quote
Reply


Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump


All times are GMT -5. The time now is 06:41 AM.


Powered by vBulletin® Version 3.8.3
Copyright ©2000 - 2024, Jelsoft Enterprises Ltd.